Experimental Investigation on Perfor

時間:2023-04-27 18:57:22 航空航天論文 我要投稿
  • 相關推薦

Experimental Investigation on Performance of Pulse Detonation Rocket Engine Model

The PDRE test model used in these experiments utilized kerosene as the fuel, oxygen as oxidizer, and nitrogen as purge gas. The solenoid valves were employed to control intermittent supplies of kerosene, oxygen and purge gas. PDRE test model was 50 mm in inner diameter by 1.2 m long. The DDT (defiagration to detonation transition) enhancement device Shchelkin spiral was used in the test model.The effects of detonation frequency on its time-averaged thrust and specific impulse were experimentally investigated. The obtained results showes that the time-averaged thrust of PDRE test model was approximately proportional to the detonation frequency. For the detonation frequency 20 Hz, the time-averaged thrust was around 107 N, and the specific impulse was around 125 s. The nozzle experiments were conducted using PDRE test model with three traditional nozzles. The experimental results obtained demonstrated that all of those nozzles could augment the thrust and specific impulse. Among those three nozzles, the convergent nozzle had the largest increased augmentation, which was approximately 18%, under the specific condition of the experiment.

作 者: LI Qiang FAN Wei YAN Chuan-jun HU Cheng-qi YE Bin   作者單位: School of Engine and Energy, Northwestern Polytechnical University, Xi'an 710072, China  刊 名: 中國航空學報(英文版)  ISTIC 英文刊名: CHINESE JOURNAL OF AERONAUTICS  年,卷(期): 2007 20(1)  分類號: V2  關鍵詞: pulse detonation rocket engine   impulse   nozzle   experimental investigation  

【Experimental Investigation on Perfor】相關文章:

Rolling Control Characteristic Experimental Investigation of a Canard Missile with Free-Spinning Tail04-27

Experimental study on Cr(Ⅵ) reduction by Pseudomonas aeruginosa04-25

Experimental study on the simultaneous desulfurization and denitrification by duct injection04-25

Experimental study on the interaction of fine water mist with solid pool fires04-27

Investigation of the Aerodynamic Character in Turbine Cascades with Aft-loaded Profile04-26

Investigation into debris cloud characterizations for oblique hypervelocity impact of projectiles on bumper04-27

Experiment and mechanism investigation on advanced reburning for NOx reduction: influence of CO and temperature04-27

Experimental approaches and analytical technique for determining heavy metals in fallen dust at ferrosilicon production04-25

INVESTIGATION OF WO3-DOPED TiO2 FILM COMPOSITE PHOTOCATALYST04-26

Experimental studies on electrical breakdown field strength of electrode with water mist containing MC additives04-27

国产v亚洲v天堂无码网站,综合亚洲欧美日韩一区二区,精品一级毛片A久久久久,欧美一级待黄大片视频
精品视频一区二区自拍 | 日本中文字幕乱 | 制服丝袜在线观看亚洲不卡 | 日本永久精品视频在线观看 | 日本免费无遮挡一区二区三区精品视频 | 综合高清亚洲国产 |